Browse
Search
Agenda - 11-15-2016 - 7-b - Chapel Hill Town Hall Study Committee
OrangeCountyNC
>
Board of County Commissioners
>
BOCC Agendas
>
2010's
>
2016
>
Agenda - 11-15-2016 - Regular Mtg.
>
Agenda - 11-15-2016 - 7-b - Chapel Hill Town Hall Study Committee
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
11/10/2016 12:19:23 PM
Creation date
11/11/2016 8:26:58 AM
Metadata
Fields
Template:
BOCC
Date
11/15/2016
Meeting Type
Regular Meeting
Document Type
Agenda
Agenda Item
7b
Document Relationships
Minutes 11-15-2016
(Linked From)
Path:
\Board of County Commissioners\Minutes - Approved\2010's\2016
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
22
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
14 <br /> Chapel Hill Old Town Hall Structural Assessment <br /> Page 3 <br /> We recommend that deteriorated mortar joints be repointed by an experience mason. The <br /> cause of the water leaking must be identified and corrected to prevent further damage. Other <br /> locations may also require repointing, such as at a steel lintel where the mortar had become <br /> loose due to minor rusting of the steel. At that location, the lintel should be cleaned and <br /> protected before repointing. <br /> We also observed damage to the trim of the cupola caused by exposure to water. From within <br /> the cupola, the wood framing shows evidence of exposure to moisture, but we observed no <br /> significant structural damage. Once the moisture problems have been corrected, the trim can be <br /> replaced. <br /> iiiii041000 ,, AININNIMINN ' <br /> Water damage to trim of cupola. Evidence of moisture at interior of cupola. <br /> Structural damage not yet significant. <br /> Below the lower portion of the cupola, some of the anchoring threaded rods were visibly loose. <br /> We recommend that these be tightened: <br /> y =tearz / <br /> tit -- r -'.-'_.j_ <br /> rp d <br /> A <br /> 41 <br /> View of loose threaded rod inside the cupola. <br /> In summary, it is our opinion that the overall structural condition of the building is very good. <br /> Other than the items noted above associated with moisture, we observed no visible evidence of <br /> distress to the structure. <br /> illI LHC STRUCTURAL ENGINEERS <br />
The URL can be used to link to this page
Your browser does not support the video tag.